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August 23, 2003

Shearon Harris: One of the most troubled reactors in the U.S.
In August, NC WARN revealed that EIGHT system failures at the Shearon Harris nuclear plant have occurred since April.  Progress Energy stated there were only FOUR.  (See list on page 2)

The Discrepancy:
The NRC uses a complicated and public-unfriendly formula for classifying and reporting “SCRAMS”, also called “reactor trips,” “unplanned shutdowns,” etc.  In a nutshell, a multitude of human and mechanical problems, along with acts of nature, can require the reactor to be shutdown automatically or manually in order to avoid overheating.

Some of this year’s eight system failures at Harris occurred while the reactor was off-line for refueling in April and May, and as it was being powered back up afterward.  Some of these are not classified by the NRC as a SCRAM, even though if they had occurred with the reactor running, each would have almost certainly caused it to trip. 

All eight failures exceeded the NRC’s “event” reporting level, and each required back-up safety systems to engage.  Even when the reactor is off-line, the cooling system must exhaust large amounts of excess heat from the reactor core and waste pools.

In fact, the margin for safety can be far lower during many points of a refueling outage than during normal operations; the reactor vessel and containment building are often open, other safety systems aren’t always in place, and handling of fuel creates particular risks.  NRC studies show that one particular 24-hour function during refueling involves risk equal to that incurred during 37 days of normal plant operations.  We believe the most serious of Harris’s eight failures occurred at that time
(see April 26 below). 

From NRC reports and Progress statements, it appears that the causes for most of the emergency shutdowns remain unknown.  Each failure diminishes safety margins, and opens the possibility for further errors that could lead to core damage.

The industry average for narrowly defined SCRAMs is one per 27 months.


So even if one only compares Harris’s four actual SCRAMS in 2003, along with four more last year, Shearon Harris’s problems are running ten times over the industry average since 2002, when there were four additional SCRAMS.

As UCS Nuclear Safety Engineer David Lochbaum points out, Three Mile Island had 12 recurring cooling system failures – which plant owners didn’t understand or correct – in the year preceding the April 1979 meltdown.

“Non-Nuclear” Failures?
Progress Energy told the media the recurring problems are on the “non-nuclear” side of the plant and did not involve the cooling system protecting the reactor.  If that were true, the Nuclear Regulatory Commission would not have sent a special inspection team to Harris.

The various loops of the cooling system are interconnected, and together must exhaust large amounts of heat in order to avoid damage to the reactor core.  At Harris, that cooling system also serves the high-level waste pools.

History’s two worst nuclear accidents started on the “non-nuclear” side. Turbine testing led to the 1986 Chernobyl explosions.  The “non-nuclear” condensate system at Three Mile Island failed, leading to partial meltdown of the nuclear core.

System Failures at Shearon Harris in 2003:

April 26  A relief valve failed, causing interruption of core cooling early in the refueling process.  A special two-week investigation by an NRC team found that had cooling not been restored, water inside the reactor would have boiled in 29 minutes.  NRC said workers could have closed containment hatches in 25 minutes to prevent radioactive steam being released into the atmosphere, then started a pump to replace the water being boiled off from around the reactor core.                                                                                     

May 16  Restart of the reactor after refueling was delayed when a back-up cooling pump was activated during testing of the primary cooling system. 

May 18  A turbine trip activated back-up cooling pumps and caused shutdown of the reactor as it was being powered back up.  

May 20  Failure of operating main feedwater pump activated back-up cooling pumps and caused shutdown of the reactor.  

May 22  The reactor was at 72% power when it tripped again due to vibrations in the main cooling water system. 

June 14  Pump malfunction in the main feedwater system led to shutdown of the reactor. 

June 15  Human error led to failure in the same cooling system as the plant was preparing to be brought back on line. 

August 17  Pump failure in the condensate portion of the cooling system causing a second pump to fail.  Plant operators shut the reactor down in anticipation of an automatic shutdown. 


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Contact NC WARN:

North Carolina Waste Awareness and Reduction Network
P.O. Box 61051, Durham, NC  27715-1051
Ph: (919) 416-5077     Fax: (919) 286-3985


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